Who knew that a tiny quadcopter could be mischeavous. When we thought there was one mode, there were two. When we thought we needed more power for the quad, it comes in and it weighs too much and we can’t even connect the battery to the quadcopter. We tried to pull off a weight test, the controller does not work. So, we are looking at a quadcopter that has the capability to be awesome, but is lagging communication and needs power. We had a little meeting, and we are thinking about redoing the whole quadcopter to make it work again. What we are going to do in class is meet up and discuss what needs to be fixed. Then we shall complete these tasks and have a successful project, or whatever is left that can be successful.
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Let’s go over this in class and see what we can come up with as a work around so you aren’t waiting for parts.