Week 16 Journal Entry

This past week, we decided to take the quad rotor project in a different direction. We decided that it would be best to setup a code on the arduino board to spin four motors. We re-soldered the wires on each rotor. we stuck the other end of the wires into the arduino board and our idea worked. The arduino board was able to power each rotor enough to make them spin continuously. In the process of doing this, one of the rotors came off the helicopter. This week, we will try to reattach that rotor, but if we can’t it’s ok because it isn’t important to our project. We also have to complete the video and blog for the project.

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